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程潮铁矿东付井原有摇台,不仅笨重(约215公斤)用人工操作不方便,而且摇台伸出之轨道尖容易损坏,经常发生故障,需要更换修理,对井下施工的运料及出渣影响很大,过去一直被认为是井下运输的难题。改为自动化摇台后.具有轻便灵活(总重20公斤)、不需人工操纵和不易损坏耐用等优点。缺点是:对罐准确度要求很高,稍有误差矿车在推上罐笼时便会产生冲击,使罐笼及罐道木受到一定影响。因此除要求卷扬司机具有熟练的操作技术外,还需作进一步的研究改进。自动化摇台制作情况是在罐笼的轨道前端各装弹簧一个,夹板两块、活动弧形搭桥一个,在马头门轨道前端各装一块弧形板,对罐时,活动弧形搭桥与马头门弧形板间隙在10毫米左右,以
The original cradle of the east pay well of Chengchao Iron Mine is not only cumbersome (about 215 kg), but is inconvenient for manual operation. Moreover, the orbit tip of the cradle is easy to be damaged and often fails. It needs to be replaced and repaired, Large, the past has been considered a problem of underground transport. After the change to automatic cradle, with light and flexible (total weight 20 kg), without manual control and easy to damage and other advantages of durability. Drawbacks are: the accuracy of the tank is very high, a slight error in pushing the tank on the car will have an impact, so that the cage and the tarmac is subject to a certain extent. Therefore, in addition to winch drivers require proficiency in the operation of technology, but also for further research and improvement. Automatic cradle cradle production is in the cage front of the spring loaded with a spring, two splint, activity arc bypass a, in the front of the head of the horse head door fitted with a curved plate, the tank, the activities of the arc bridge and the horse head Door arc plate clearance of about 10 mm