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辽河油田的试验表明,将破乳剂AP_(8051)与SP_(169)复配使用,并选择恰当的加药位置及相应的工艺流程,可使破乳温度从60℃降至40℃甚至35℃,实现原油降温脱水,达到既减少投资又节约能源的目的。
The experiment of Liaohe Oilfield shows that demulsifying agent AP_ (8051) and SP_ (169) can be used in combination with proper dosing position and corresponding process to reduce the demulsification temperature from 60 ℃ to 40 ℃ or even 35 ℃ , To achieve cooling oil dehydration, to achieve both reduced investment and energy conservation purposes.