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三明化工厂有合成氨、电石、热电、机械等5个分厂。全厂设备近3300台,其中受压容器531台。根据化工生产高温、高压、易燃、易爆、有毒的特点,我们认真执行化工部、国家劳动总局有关受压容器的安全监察条例和规程,确保全厂生产的安全。 一、领导重视、机构健全是搞好受压容器管理的关键 合成氨厂是“文革”期间上马的厂,建厂初期对受压容器管理不够重视,给安全生产带来严重威胁。碳铵装置的加压变换炉1970年底投产,因容器接管的筒体没有焊牢,只在加强板外圈与筒体焊接,在检验中,又未作加强板的试漏检查,在生产中,又出现漏孔冒“兰
Sanming chemical plant ammonia, calcium carbide, thermoelectric, machinery and other five branches. The whole plant nearly 3300 units, of which 531 containers under pressure. According to the chemical production of high temperature, high pressure, flammable, explosive, toxic characteristics, we conscientiously implement the Ministry of Chemical Industry, the State Administration of labor safety regulations for pressure vessels and regulations to ensure the safety of the entire plant. I. Leading attention and sound organization are the key to managing pressurized containers Ammonia plant was launched during the “Cultural Revolution”. The initial construction of the plant did not pay enough attention to the management of pressure vessels, posing a serious threat to safety in production. Ammonium bicarbonate plant conversion furnace put into operation by the end of 1970, because the container is not welded tube body welded tube, only in the outer ring of the reinforcement plate welded with the cylinder, in the test, but not for enhanced leak test board inspection, in production , There are leaks to take "blue